Victor A. Yangali-Quintanilla
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4 records found
1
The objectives of this study are to assess the performance of antiscalants in increasing the recovery (≥85%) of a reverse osmosis (RO) plant treating anaerobic groundwater (GW) in Kamerik (the Netherlands), and to identify scalants/foulant that may limit RO recovery. Five different commercially available antiscalants were compared on the basis of their manufacturer-recommended dose. Their ability to increase the recovery from 80% to a target of 85% was evaluated in pilot-scale measurements with anaerobic GW and in once-through lab-scale RO tests with synthetic (artificial) feedwater. A membrane autopsy was performed on the tail element(s) with decreased permeability. X-ray photoelectron spectroscopy (XPS) analysis indicated that calcium phosphate was the primary scalant causing permeability decline at 85% recovery and limiting RO recovery. The addition of antiscalant had no positive effect on RO operation and scaling prevention, since at 85% recovery, permeability of the last stage decreased with all five antiscalants, while no decrease in permeability was observed without the addition of antiscalant at 80% recovery. In addition, in lab-scale RO tests executed with synthetic feed water containing identical calcium and phosphate concentrations as the anaerobic GW, calcium phosphate scaling occurred both with and without antiscalant at 85% recovery, while at 80% recovery without antiscalant, calcium phosphate did not precipitate in the RO element. In brief, calcium phosphate appeared to be the main scalant limiting RO recovery, and antiscalants were unable to prevent calcium phosphate scaling or to achieve a recovery of 85% or higher.
The potential of membrane scaling control by a real-time optimization algorithm was investigated. The effect of antiscalant dosing was evaluated from the induction time measured in glass batch-reactors, and from the operational performance of a lab-scale reverse osmosis (RO) unit and two pilot-scale RO units. Step changes in the antiscalant dosing demonstrated that the accumulation of scaling is ‘paused’ during periods when the optimum dose is applied. This is paramount for the application of a dynamic dosing strategy that may briefly underdose, while searching for the optimum dose. It was found that antiscalant underdose and overdose were both detrimental to RO operation since underdose resulted in membrane scaling, while overdose led to membrane fouling due to calcium-antiscalant deposits. The dosing algorithm was used to minimize antiscalant consumption in two pilot RO units. The algorithm was able to lower the antiscalant doses to 0.2 mg/L and 0.6 mg/L, while the supplier's recommended antiscalant doses were 2.0 mg/L and 4.5 mg/L, respectively. As a result, the algorithm could reduce antiscalant consumption by up to 85–90% for the plants mentioned.
The role of phosphate and humic substances (HS) in preventing calcium carbonate scaling and their impact on antiscalant dose was investigated for a reverse osmosis (RO) system treating anaerobic groundwater (GW) (containing 2.1 mg/L orthophosphate and 6-8 mg/L HS). Experiments were conducted with the RO unit (treating anaerobic GW), and with a once-through lab-scale RO system (operating with artificial feedwater). Additionally, (batch) induction time (IT) measurements were performed with, i) real RO concentrate, and ii) artificial RO concentrates in the presence and absence of phosphate and HS. It was found that at 80% recovery (Langelier saturation index (LSI) 1.7), calcium carbonate scaling did not occur in the RO unit when the antiscalant dose was lowered from 2.2 mg/L (supplier's recommended dose) to 0 mg/L. The IT of the real RO concentrate, without antiscalant, was longer than 168 h, while, at the same supersaturation level, the IT of the artificial concentrate was approximately 1 h. The IT of the artificial concentrate increased to 168 h with the addition of 10 mg/L of phosphate, humic acid (HA), and fulvic acid (FA). Furthermore, in the lab-scale RO tests, the normalized permeability (Kw) of the membrane decreased by 20% in 2 h period when fed with artificial concentrate of 80% recovery containing no phosphate, whereas, with phosphate, no decrease in Kw was observed in 10 h period. These results indicate that phosphate and HS present in the GW prevented calcium carbonate scaling in the RO unit and reduced the use of commercial (synthetic) antiscalants.
Hybrid SBR-FO system for wastewater treatment and reuse
Operation, fouling and cleaning
Forward osmosis (FO) is a novel membrane separation process that potentially can be used as an energy-saving alternative to conventional membrane processes. A hybrid sequential batch reactor (SBR)-FO process was explored. In this system, a plate and frame FO cell including two flat-sheet FO membranes was submerged in a bioreactor treating synthetic domestic wastewater. The dissolved organic carbon (DOC) removal efficiency of the system was 98.55%. Total nitrogen removal was 62.4%, with nitrate, nitrite and ammonium removals of 58.4%, 96.2% and 88.4%, respectively. Phosphate removal was almost 100%. The 15-hour cycle average water flux of a virgin membrane with air scouring was 2.95L/m2·h-1. Air scouring can help to remove loose foulants from the membrane active layer, thus helping to recover up to 89.5% of the original flux. Chemical cleaning of the fouled active layer of the FO membrane was not as effective as air scouring. Natural organic matter (NOM) characterization methods (liquid chromatography-organic carbon detection (LC-OCD) and 3-D fluorescence excitation emission matrix (FEEM)) show that the FO membrane has a very good performance in rejecting biopolymers, humics and building blocks, but a limited ability in rejecting low molecular weight neutrals. Transparent exopolymer particles (TEP) and other biopolymers might be associated with fouling of the membrane on the support layer. A 1% sodium hypochlorite (NaOCl) cleaning solution was proved to be effective for removing the foulants from the support layer and recovering the original flux.